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Paul Richards

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Posts posted by Paul Richards

  1. After much trial, I finally sought the services of a mobile auto electrician who carried out similar tests and he was equally baffled. We were just coming to the conclusion that there must be a problem with the wiring and having checked it all except under the dash I was envisaging having to remove the scuttle to get at it all. We finally made one last check and removing the offside led rear stop tail bulb cut the 6.7 volts going to the brake circuit. Replaced the bulb and and hey presto all working fine. 

    Couldn't believe that a bulb could go faulty like that and be responsible for such a failure.

    Happy boy now *biggrin*. Now off to celebrate St. Pats day with a drop of Guinness.

  2. The clips have little barbs on them. You'll probably have to prise them off with a screwdriver. They probably won't be reusable. I find it better to secure by drilling a couple of small holes either side of the slots and using a small cable tie to secure. Drill the holes so that the cable tie puts a little tension on the grill tang. IYSWIM

  3. No progress I'm afraid. Various tests undertaken and no success. Currently no time to spare. Fortunately car is functional with only sympton being a slight glow on high level brake light when sidelights on. 

    I'll try and find time in a couple of weeks. 

  4. When my sidelights are on the high level LED brake light (connected to nearside using Caterham sub loom) glows. Meter shows that there is 6.7 volts in the brake light wiring.

    Most likely to be a bad earth. I've checked the earth on the wiper motor frame and all is OK. Are there any earths in the sidelight/brake light loom and if so where are they located?

  5. In the past I've tried using grease to hydraulically remove the spigot bearing from the crankshaft with no success. I've then ended up slide hammering, chiselling, prodding and generally "botching" the spigot bearing and shim out.

    I can't claim credit for this new method as it was recommended to me by another member of LADS. I've now used this method twice and it works extremely well so I thought I'd share it with you.

    It's just the same method as using grease, but instead use very tiny bits of newspaper which have been thoroughly wetted in water. 

    Take the tiny paper shreds and drop into a bowl of water and let them soak for a few minutes. Once wet, push the paper into the spigot bearing and then using the end of your clutch alignment tool hammer in the paper. Add more paper if necessary and repeat and voila out pops the bearing. 

    Hope this helps.

  6. You've got it easy. Seats were originally fixed by hex head bolts and you had to jam the head in the runner with a screwdriver. 

    I now find the best thing to do is weld the bolts to the runners. Then it's an easy job to remove and replace the seats by just removing the nuts from underneath. 

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