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New build - HG Failure


Racingshoe

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My 1900k has been with a specialist these past few weeks getting installed and ready to run. The engine was built a year ago, but has sat unused (we had a baby in the meantime) until now. I got a phone call last night to say that it had dropped a load of coolant out of the exhaust, which seems like HG failure to me.

 

What would cause this on a brand new engine, and one with a Scholar block ? Bear in mind that this was an initial startup, so low revs...... *confused* *mad*

 

Rik Robarts - bl**dy bright orange 1900k here

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Bad news indeed. I am revising at the moment ☹️, so car is up in Cheltenham. Have not had a chance to look at it yet.

Really really getting fed up with the whole thing now. Almost at the point of digging a hole in the garden and burying the fecking thing.

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Rik,

 

I have seen this before, some of the steel head to block dowels supplied with the uprated head gaskets were too long thus not allowing the head to seat properly. If the head was porous it would only be a a very small weep of coolant . You have my sympathy.

 

Rob

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Rik - my 1900 did exactly the same and it turned out to be the steel dowels that came with the head gasket were too long. Luckily we had the plugs out to crank for oil pressure - you should have seen the coolant shoot out all over the walls of Dave Andrews' garage *eek*.

When you strip it back down, make sure the head has not warped - we did that using a "guaranteed straight edge" that Dave had and I was lucky otherwise you will need the head skimmed again.

I wonder if the fact that Scholar machine the top of the block means that the locating holes are not as deep. Add to that the fact that a lot of tuned engines will have skimmed heads means that the dowels are just too long.

You will need to reduce the length of the dowels and also perhaps put a bit more of a chamfer on them - Dave did that for mine and the engine went back together with no issues.

 

Yellow SL *cool* #32

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Have you been able to confirm the rings that are in your engine ?.

 

Its pointless starting it up if it has the original troublesome Pistal rings that were in circulation at the time you purchased the scholar block. If you start it and run it and have a problem with the rings you will then have to hone the block and increase your clearances etc and still fit new rings ☹️.

 

a leak down test should diagnose the scource of the coolant loss *thumbup*

 

Dave

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